This document discusses the implementation of the Six Sigma quality improvement methodology in a local manufacturing company producing pump casings, which faced a high rejection rate of 25%. The study details the DMAIC (Define, Measure, Analyze, Improve, Control) approach used to reduce the rejection rate to an acceptance limit of 1%, along with various statistical analyses conducted during the process. Key statistical tools and techniques, such as control charts and process capability indices, are highlighted as critical in monitoring and improving quality.
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